• The site migration is complete! Hopefully everything transferred properly from the multiple decades old software we were using before. If you notice any issues please let me know, thanks! Also, I'm still working on things like chatbox, etc so hopefully those will be working in the next week or two.

2000 Daytona





no KR after fuel pump, nice...

pretty funny everyone was instantly on the band wagon to blame zzp for the KR spikes... lawl ROFLMAO
 
no KR after fuel pump, nice...

pretty funny everyone was instantly on the band wagon to blame zzp for the KR spikes... lawl ROFLMAO

Haha yea I've just heard to many horror stories and didn't want to be another statistic. I'm happy everything's been running okay, but I'm retuning for corn soon anyways lol
 




Well everybody. I have some bad news.

Anmar is too depressed to come on this site and update what happened this previous weekend.

Both me and him were on poopy tunes, so we decided to get re-tuned. This was a great opportunity for Anmar to go e85. Remember he has, Stage 2 ported heads, over-sized valves, NIC cam, LS1 TB, LQ4 Maf, Racetronix fuel pump, 60# injectors, High comp block, Gen V, and a brand new fully built trans with 7/8th chain, 300m, hardened 4th blah blah blah. Decent setup.

He gets convinced to run a 2.8" with e85. We throw on the 2.8" and off to tuning for e85 he went. Car ran well with it and knock free the whole time. BUT on a WOT pull, the car leaned out and popped two pistons. Either the LQ4 or the fuel pump got maxed out on the setup and chipped two pistons.

The car still runs and drives, unsure if there is compression loss in the cylinders. But Anmar has had enough with the car, to much money dumped into it, and problems keep happening. He is going to sell the car as is, there is no part out on this.

The end.
 
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